What everyone's up to

Oct 24, 2021
Worked on a project car
Worked on an air-cooled VW
It's been six weeks since I last shared an update on my Karmann Ghia project, but that doesn't mean I haven't been working on it; in fact, the car's had one end or the other on jackstands for most of that time.

I drove the car to work one day following my last update, and when I got home I realized that the front-left wheel was radiating a lot of heat, while the front-right was only slightly above the ambient temperature. I removed the wheel and discovered that the caliper was seized and dragging the outside pad, which was about half as thick as the inside pad. I found a caliper rebuild kit for about $40, but I'd still need new pads (even assuming that I could successfully rebuild the bum caliper) - or I could spend $200 for a pair of new calipers with fresh pads included. I also ordered a new pair of brake hoses since the ones that were on the car were a bit worse for wear, and threw in a bunch of other small parts I'd been meaning to order as well.

When the parts arrived, I set to work replacing the hoses and calipers. That was going well until I stripped the fitting securing the hard line to the flexible hose. I realized I would have to instead remove the other end of the hard line where it connects to the brake cylinder, so I ordered  a new hard line as well.

While I waited, I installed some of the other parts to correct some minor deficiencies:
  • Replaced broken window crank handles to make it much easier to roll the windows up and down.
  • Installed (missing) carburetor pre-heat hose to feed the carb warmer air from underneath the engine until the engine bay is warmed up.
  • Replaced cracked carburetor intake hose.
  • Installed (missing) heater hoses to connect the cabin vents to the heater box under the engine.
  • Replaced broken heater cable to control the flaps closing the heater box off from the hoses leading to the cabin vents. Of course, I also found that the car was missing the levers to actually connect the flap controls to the cable so I had to order a pair of those as well.
  • Replaced (broken/missing) engine lid release cable. Also discovered that I needed some sort of guide tubing to feed the cable through so I raided a hardware store for some semirigid plastic tube of the sort used for connecting an ice maker's water supply. I got it connected to the engine lid release mechanism... and then found that the lid doesn't quite line up the way it's supposed to. Ah well, I'll fight with that another day.
Once the new brake line and heater box control levers arrived I was finally able to install those, bleed the brakes, and crank the engine for the first time in over a month (it started up fine!) and go for a test drive. 

It stops much better with the new brakes! Rolling up the windows so I can lock the car once I get to where I'm going is much easier now. Hopefully the reconnected heater components will help keep me comfortable when it's chilly outside, and hooking up the carburetor preheat should help the Ghia deal with the cooler weather as well. I'm so glad to have this car back on the road, and can't wait to drive it again!



Sep 11, 2021
Worked on a project car
Learned something
Worked on an air-cooled VW
+ 1
It's been a fairly productive Ghia week!

  • Remember how I don't really know what I'm doing? That was confirmed this week when I realized that I'd basically been doing everything wrong. For some reason, I had (incorrectly) assumed that the single notch on the rear portion of my crank pulley must mark Top Dead Center, when the piston is fully extended inside the cylinder; I then read something that suggested the notch instead indicated 7.5 degrees Before Top Dead Center. To check this, I removed the spark plug from cylinder 1, stuck a plastic straw inside as a feeler, and slowly turned the engine with a 21mm wrench applied to the alternator pulley. That let me feel when the piston stopped moving... and, sure enough, it wasn't when the notch was lined up with the crack on the case. In fact, this position matched with the hard-to-see dimple on the front portion of the pulley. Good to know! 
  • Of course, that also meant that my previous valve adjustments had been performed incorrectly; those are supposed to be done with each piston in its TDC position - not 7.5 degrees before. So I re-did those adjustments, and it only took about fifteen minutes this time! It didn't make a big difference, but there were a couple of cylinders that had just a wee bit (like 0.008" instead of 0.006") too much valve gap. 
  • And I think I've finally figured out what I'm doing with regards to timing the (aftermarket) 009 distributor which was installed in the car at some point. All the specs I found said to time it to ~10 degrees BTDC at idle. Since the 009 isn't equipped with vacuum advance (it just centrifugally advances the timing as it spins faster), it's actually way more important to set the peak advance to about 32 degrees at around 3500 rpm; that should drop to 5-10 degrees BTDC at idle, but the exact timing isn't as important here. I printed out a timing wheel and used that to mark the relevant points around the rim of the crank pulley (TDC, a range covering 5-10 degrees BTDC, and a hash to mark the 32 degree maximum advance).
  • And I discovered that the Innova 3340 tach/dwell (many other functions) meter I'm using seems to do a much better job of reading the RPMs when I use the inductive pickup on the cylinder 1 spark plug wire and put the meter in indistinctly-named "CON" mode rather than attaching the contact probe to the negative terminal on the coil and setting the meter to "RPM" mode. It had previous been pretty tough to read, and often indicated that the car's idle was set way too high. The measurements are much more consistent (and reasonable) when using that inductive pickup.
  • So I combined all of this knowledge to actually get the timing set correctly (finally!), with a maximum of about 30 degrees advance at 3500 rpm and a comfortable idle of 7ish degrees BTDC at ~850 rpm. 
  • And I used the improved RPM measurements to also tweak the carburetor settings a bit, per the Bentley manual: I used the big bypass screw to set the idle to about 850 rpm, turned the smaller volume adjustment screw until the engine ran at its fastest and kept turning clockwise until it dropped off ~30 rpm, and finally used the big bypass screw to reset the idle at about 850. So maybe the car is now tuned correctly?
  • I had intended to drive the Ghia to work on Thursday since the weather was going to be nice, but my pre-flight check that morning revealed that the brake lights weren't working anymore. That evening, I jiggled some wires and got them working again... hardly a proper fix, but enough to take the Ghia to work on Friday - which I did! It drove like a dream.
  • Today, my wife and I spent a few hours cleaning up the electrical connections for the front and rear signal lights. I was a bit surprised to find that each bulb only had a single wire running to it, relying on the light housing itself to provide the connection to ground and complete the circuit. We carefully cleaned the corrosion and grime off of the wiring connections and thoroughly cleaned the bulb sockets as well. Once everything was put back together, all the lights worked again (yay), and some of them even glowed more brightly than before. Hopefully this cleanup will help keep the current flowing better in the future. We plan to revisit the other end of those wires (at the fuse box behind the dashboard) soon.
I feel a bit silly for having been doing things fairly wrong so far, but I'm glad to have finally figured things out. I learned a lot this week, and the Ghia is running beautifully. I think we'll take the Ghia out for more joy rides and trips across town now that the weather is (maybe?) cooling off a bit and we're getting a bit more comfortable and confident with the car's transport abilities. 
Sep 05, 2021
Worked on a project car
Worked on an air-cooled VW
Now I've got a drain plug!

I noticed that the Ghia had been leaking a bit of oil in the past couple of weeks, probably because I hadn't been adequately prepared for that first tuneup and had reused the existing gaskets for the oil screen and the sump plate. I ordered several sets of gaskets, and also picked up an aftermarket sump plate with a built-in drain plug. That should make future oil changes much easier!

Plus it's shiny so that's +5hp.

I also did a bit of fiddling with the timing and carburetor settings. I realized that my car doesn't have the factory-correct single-vacuum double-advance (SVDA) distributor and instead has an aftermarket Bosch 009 unit with no vacuum advance (centrifugal only). The specs say that I should set the timing for that to ~10BTDC, but the motor really didn't seem to like that. No amount of adjustment on the carburetor would get it to idle correctly. I kicked the timing back to the ~5BTDC I was using previously and I was then able to adjust the idle with the bypass screw and the mixture with the volume screw. It seems happier now.

I'm not sure why the timing would need to be set so far off from what everything I can find suggests the 009 should be, but of course I also don't know what else might not be factory-stock about this motor. 

But hey, I'm learning stuff and enjoying the car along the way!
Aug 28, 2021
Worked on a project car
Worked on an air-cooled VW
Another lovely weekend day, another couple of hours of wrenching on our 1974 VW Karmann Ghia...

  • We rechecked the toe alignment on the front end, and found that I'm a dumb-dumb and my previous alignment efforts hadn't been accurate since the suspension wasn't loaded. Rather than using a laser pointer held against the hubs, this time I used a pair of yardsticks held up between the inner edges of the rims stretching from one side of the car to the other. I marked where the sticks overlapped with the measurement taken between the front edge of each wheel and again between the rear edge. This revealed the car was actually sitting with about 1/2" toe out, which likely explains why I was having to fight so much to keep it centered on the road. I eventually got it dialed in to about 1/8" toe in.
  • I had to raise the front end again in order to get at the lock nuts on the inner tie rod ends, and along the way I noticed that the passenger side wheel had a little bit of side-to-side play in it. I removed the cap on the center of the hub and tightened the wheel bearing adjustment nut to eliminate the slop. I did the same on the driver side for good measure. 
  • I then lifted up the rear of the car to see about adjusting the drum brakes, which I suspected weren't releasing all the way. It turns out I was right: even with both wheels off the ground, I couldn't turn the left rear wheel on my own. I used a flat-head screw driver to spin the shoe adjustment star wheel things and got the wheel to rotate more freely. I dialed them back down until the wheel started getting some resistance, and backed off just enough to spin freely again. I repeated this for the right drum as well.
  • While I was under the rear of the car, I also identified a disconnected wire that had been dangling beneath the car (and driving me nuts every time I saw it). It's the starter end of the stock ignition circuit - so there's another explanation for why I can't start it up by turning the key and must instead press the button behind the passenger seat. I had hoped that I could just reconnect it to the starter and get back in business (and even confirmed that the wire gets +12VDC when the key is turned to the "start" position) but it still wasn't doing the trick. I reconnected the bypass circuit between the battery, the button, and the starter, and at least used a wire tie to keep the stock wire from dangling in the future.
  • My wife also spent some time removing the black vinyl wrap a previous owner had used to cover up the chrome trim pieces on both sides of the car. The chrome underneath is a little scuffed, but we both think that the lines look a lot better (even if some of the lines aren't completely straight...).
We went for a few short drives along the way to check our progress. The steering feels MUCH better; no more weird oscillation when making minor inputs. Brakes also feel better; the car stops well and it doesn't feel like the brakes are still applied when I lift off the pedal. 

All told we put another 15 miles on the car today, and I'm really enjoying the way it drives now. I can't wait to drive it to work again - once it cools off a bit more.
Aug 23, 2021
Worked on a project car
Worked on an air-cooled VW
I did it! I drove the Ghia to work!

Perhaps more importantly, I also drove it home! My previous drives had all been little 5-mile circuits around the house, so doing ~30 miles round-trip feels like a great confidence-boosting accomplishment. Now I know that the car (and driver!) is up for cross-town trips.

The longer drive also revealed a few things that I'd like to investigate further. After a bit of hard braking, it felt like the rear drum brakes may not be retracting quite far enough when I lift off the pedal. I'll take a look at adjusting those rear shoes this weekend, and will likely go ahead and replace the fluid as well for good measure.

I also found that, while the car tracks nice and straight with no steering input, if I provide a small input to better center the vehicle in the lane I generally have to deliberately counter that input rather than just letting the steering come back to center, and this is compounded by the well-within-spec inch of free play in the steering wheel. It can wind up taking quite a bit of effort to effectively counter the small initial input without resulting in a nasty bout of pilot-induced oscillation... and that's kind of scary. I'm not sure yet if this is indicative of a problem with the car (alignment? bad steering damper? something else?) or a problem with the driver just not being used to how old cars steer. I'm going to try to do a better driveway alignment and see if I can get the toe dialed in a bit more accurately; if not, I'll get to a shop for a professional alignment and figure out where to go from there.

Overall, I think the drive was a resounding success! That said, 30 miles round-trip in sunny 90°F+ humid Alabama weather without any air conditioning wasn't the most comfortable way to travel. I was pretty ripe by the time I got to the office, and riper still when I finally reached home. I don't think the Ghia will be a regular commuter vehicle for me until outside cools off significantly. I look forward to that happening though!
Aug 22, 2021
Worked on a project car
Worked on an air-cooled VW
Today my wife and I spent some time doing some tuneup work on our 1974 VW Karmann Ghia:

  • Adjusted valves with a 0.006" feeler gauge
  • Adjusted distributor points to ~49° with a dwell meter
  • Adjusted timing to 5° BTDC with a timing strobe
  • Changed oil
  • Changed spark plugs
The engine already ran pretty well, but it runs even better now! I'm very pleased with that result since this was our first time ever doing the first three items on the list. 

It was really great to learn a bit more about how this engine works in the process. Being able to easily turn the engine with a wrench really helped me to better understand how the pieces fit and work together. And making adjustments on the distributor, observing how the engine changes in response, and also seeing how it compares with the indication from the timing strobe was super cool to me.

The weather looks like it should be nice tomorrow so I'm going to try to drive the Ghia to work. It should be interesting!
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